Having just read the thread we have just been through this procedure with a satisfactory outcome. Initial problems where switching on a florescent tube, tool grinder, clicking stop button on Mach3 the U.S.B. Led would go out, pro gramme not responding. Only way out to reload windows & start agn. The mains power supply was fed from the house. Having 3 phase in the workshop a new supply for the computer was installed from L1 this used for the computer and stepper drives. The auxiliary relay box with its own P,S. fed from L3. When switching off the same result. In my build a mains filter is fitted to each transformer supply also in series with the aux. relays a thermistor of 4-5 amps current with a 100 ohm & 0.1 across the contacts( Mill, Vacuum waste, Vacuum table. ).
Using the computer case as a central point, connect an earth wire to the smooth stepper metal box, stepper P. S. and drives. In my case removing the smooth stepper C4 & R5 made no difference. A new U.S.B. cable was fitted but no difference . Fitting a suppressor across the manual switch cured the tool grinder,the motor being a capacitor start motor, before when switching off, would knockout Mach3 you could even see this on the red disc drive l.e.d. One mod worth doing is fitting a 25- 50 mf. condenser across the common feed going to the smooth stepper end of travel limits input. When these micro switches where gently tapped with a handle of a screwdriver out goes Mach3 so with the mill & steppers in operation a small amount of vibration could cut mach3.
Its a job to quantify but the main improvement in my case was fitting earth leads from the computer case to each item, mach3 would still knock out but the Red U.S.B. flashing feed light still good. Fitting the suppressors across switchable items cured the crashes , its now a reliable machine.